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Reggie Racing Page 2
Reggie recently joined Bracket Masters Racing Team and is a great
addition to our group. Reggie's Duster will make the 2nd Mopar in our club that's
dominated by Chevrolet's. This Big Block 440 Duster is consistent
and can always be counted on to go a few rounds. Reggie has been
racing for a lot of years and is a protégé of Mr. Hank Robinson (Mr.
Mopar in Baton Rouge). Reggie literally grew up in Hank's shop and
has acquired a lot of the knowledge from the racers that are in and out of
the shop. Reggie is an excellent mechanic and a very wise and
knowledgeable racer. He has done the majority of the work on all the
engines that the car has run. Reggie is an avid follower of NHRA
professional racing and attends at least one National Event each year
along with Divisional events in our region.
Bracket Masters Racing Team welcomes the Jackson Family: Justin, Toshia, Reggie Jr., Mrs. Viola Jackson and Mr. Reggie, Sr.
Sept. 2001 - The engine in the Duster was recently rebuilt and is in
the testing stage. It is currently running in the low 11 second
range, but is expected to drop into the 10's as soon as everything is
sorted out. The car recently passed NHRA Chassis Inspection and is
ready to dip into the 9's. Reggie may suprise someone shortly.
10/21/01 - Memphis, TN. Reggie
ran a 10.66 sec. ET (best ever) before #5 cylinder expired. After
removing the heads, we cannot determine exactly what happened to the
cylinder wall. The complete wall in gone and the piston is junk and
the rod is broken. The head is not repairable above #5. All
other cylinders and parts look good. Nothing else is hurt! The
speculation is a flawed or cracked cylinder wall. This motor only
made 8 passes
before failure. (Late entry - There was a
broken Intake Valve in #5).
Reggie plans to put the old 440 CID motor back in. This motor had
been running fine for 8 years. (see entry at 3/23/02 - Racers find it hard
to go slower!)
11/11/01 - Reggie has been selected
to join the BMRT
Board of Directors and he is also assigned to the
Publicity Committee.
Justin Jackson, Reggie's youngest son, and avid racing fan, attended the regular BMRT meeting.
3/23/02 - Reggie has assembled
all of the parts to put his motor back together. It will be another
440 cid Big Block Mopar. It will have special Mopar Aluminum Heads
and some other innovations to make it perform at a higher level than the
old motor. Hank Robinson, a long time Mopar engine builder and Super
Gas/Super Comp driver, is giving technical assistance and he will assemble
the heads. Reggie is targeting the mid to high nine's. This motor will be extra special. The converter is being freshened
up and the stall speed changed to match the new Comp Cams cam. Some
interior sheet metal work has been done to make access to the transmission
easier and the engine support system was modified to limit the
travel of the motor. Reggie is really serious this time.
4/6/02 - The whole Jackson family
traveled to New Iberia, LA for the 2002 Scout-O-Rama. Although the
car was not running, Reggie installed a dummy transmission and a broken
block with water pump and distributor inserted. He also had a
cylinder head on one side with one piston inserted in one of the open
cylinders. This motor was used for "Show and Tell" for the
Boy Scouts. Reggie's idea was really great and generated a lot of
conversation during the day. Many people had never seen the inside
of a motor.
4/28/02 - The whole Jackson family,
including Reggie Jr., traveled to Memphis, TN with the team.
Everyone had a very nice time at the 1st annual Bracket Race ShootOut at
Memphis Raceway Park.
5/16/02 - The new motor has been
installed and is almost ready to breath first life. This should
happen sometime this weekend.
5/19/02 - We have a Big
Block! Those were the words of Reggie Jackson after firing off the
new motor over the weekend. Reggie was working against the clock
because he had to leave for an assignment early Monday morning. Long
time friend, advisor and Mopar engine builder, Hank Robinson, came over to
put the final touches on the engine startup. The motor sounds crisp
and clean with no leaks or other problems. Reggie's attention to
detail has paid off in the first stages of the testing. They can't
wait to get to the track this coming Friday or Saturday to get in some
real world testing.
5/25/02
- The Duster went to State Capitol Dragway for Friday Test and Tune.
Reggie came off the trailer with a 10.78 second pass, shifting at 5200 RPM
to keep it mild on the first pass. Everything worked as it should
and there were no leaks. The car had a very intense technical
inspection, requested by Reggie, to make sure the car is technically
correct. We run the cars all over the country and we want to be safe
and correct wherever we run. Reggie made one more pass in the first
round of competition, and won, but put the car on the trailer and headed
home. He and Brother Ronnie, Viola, Justin and Toshia his pit crew,
where very pleased with their efforts to build the new motor and get down
the track with no problems. It is a very satisfying feeling to help
build your own motor and have it perform the way you expect. The
next time Reggie brings the car out he will raise the shift point and let
it all hang out!
6/23/02
- Reggie and Viola attended the Annual BMRT Picnic at State Capitol
Dragway and participated the racing. The Duster ran well but due to
the close tolerances in the motor, three spark plug gaps were found to be
closed. After inserting Index Washers to move the plug tips out of
harms way, the car ran well. Minor electrical work on the line lock
circuit also took place. The picnic was a great success and enjoyed
by all.
6/29/02
- Reggie took the Duster to No Problem Raceway Park and another
unfortunate occurrence happened to the motor. During the first run,
against another Mopar, a Viper, Reggie had a great Five-O light but
couldn't hole off the charging Viper when he ran a 10.76. At the end
of the run, the RPM would not go back to normal. The motor was shut
down and several things were checked. The car was returned home and
during a check of the valves, a broken exhaust (Correction - INTAKE)
valve was discovered.
We will wait for the head removal to determine the extent of the damage
(we hope, very little, as no metal particles were found in the oil or
anywhere in the lifter galleys after the intake was removed).
7/6/02 -
Reggie and Skip removed the motor and transmission after the head on the
right side was removed and taken to Hank's Auto Performance for
investigation. The head of the exhaust (Correction
- INTAKE) valve was stuck in the valve
seat. The top of #6 piston was trashed but the head had very little
damage and will be saved by installing a new seat, guide and
valve.
7/12/02 -
Reggie is reluctant to return the motor to service without knowing why
this combination has broken two exhaust (Correction
- INTAKE)
valves when everything seems to be
OK and he cannot find a problem that tells what happened. Reggie is
in the process of calling tech. lines to question the different vendors of
the heads, valves, springs, cam, fuel pump and carburetor. The valve
company has offered another set of valves for free, but will not tell what
they found on the first failure, which was sent back for analysis.
Reggie will send this set back also. We are not naming any companies
because we do not have all the facts yet.
8/7/02 -
Received this information from Reggie. "Still
waiting to have the cylinder repaired. The valve seat needed
replacing. I talked to the manufacturers tech. rep. for the
valves that I was running. They pointed to a problem in the valve
train. I checked everything that he suggested may have caused the
problem and found nothing wrong with the valve train or setup. I
have purchased another set of valves from another manufacturer. I
hope that this solves the problem. However, to be on the safe side,
I have modified the fuel system, the ignition system and will add a
charging system to the car. After the engine is reinstalled, I will
have to make some brackets to make the charging system mount up correctly.
I hope to have the car running within the next couple of weeks."
8/11/02
- Reggie picked up the Jr. Dragster from Keith's Pro Paint & Body on
Sat. afternoon. He towed it to No Problem raceway Park for the Baby
Pro-Mod Race. The Jr. Dragsters were not running but it did get to
appear in the Cox Communication-Louisiana Drag Classic commercial that was
shot at this event. Reggie was in charge of this operation and he
instructed the kids on how to start the engine and the precautions
necessary to drive the dragster. Many children had a chance to sit
in the dragster and play with the controls.
Reggie with Jr. Dragster
9/6/02 - Reggie visited the Glen
Oaks High School Automotive Class to introduce himself and to give them
information on the NHRA Youth Education Services (YES) program. See
the Jr. Dragster Program page
for more information on YES.
If first impressions make a
difference, the Glen Oaks High School (GOHS) Automotive Class, from the
instructor, Mr. Lyons, to the fine young men in the beginning class, to
the excellent facilities, made a very favorable first impression.
Reggie, who works as a Engineering Specialist at a nuclear power plant,
has a lot of experience in what it takes to make an excellent
program. Excellence is a way of life at a nuclear facility.
Reggie gave GOHS an "A" for his first visit.
Mr. Lyons has invited the team to
visit his class whenever we are available and would like for us to speak
to his classes. The young men are all very respectable, very well mannered
and helpful. The school's program has state-of-the-art equipment and
they work on new vehicles for practice. The vehicles are donated
from different organizations around the Baton Rouge area. When the
young men finish the course, they are able to go to work in many
automotive dealerships and auto repair facilities in the area. Mr.
Lyons is a certified mechanic, and the GOHS program is the only Certified
Automotive Repair Program in the area and one of the very few in the
state.
Reggie was given a chance to
speak to Mr. Lyons' class and show a portion of the NHRA Youth Education
Services (YES) program tape to the young men. We are sure that a good
working relationship between the GOHS Automotive Program and Bracket
Masters Racing Team will develop and enhance both organizations.
9/28/02 - Reggie, helped by
Reggie Jr., installed the motor and transmission today. The start-up
should be completed late Sunday. Skip will tune the carburetor after
the startup. Reggie has been working out of town the last 2 weeks,
working long hours and this weekend was the first time he had a chance to
work on his motor installation. Reggie is using his extensive
knowledge of nuclear reactor materials to consult with one of the sister
plants owned by the electric utility he works for.
10/4/02 - Reggie was at No
Problem Raceway Park to test the rebuilt motor in the Duster on Friday
night. The car ran very respectable and sounded very good.
Reggie will be ready for the Challenge Race at the Louisiana Drag Classic
this coming weekend, October 12-13, 2002.
10/13/02 - Reggie's
Duster ran very well all weekend as he tuned up for the Team Challenge
Race between New Orleans and Bracket Masters. In the Team Challenge Race at the Louisiana Drag Classic,
Reggie ran a little
too quick in the final round and finished Runner-Up to team mate John Collins.
Reggie earned a large 2nd place trophy for his efforts. Congratulations Reggie!
11/6/02 - (Update sent in by
Reggie Jackson): Took
the car to SCD on Nov. 2, 2002. The Duster ran consistent all day
with no mechanical problems. Driver needs to get back to cutting
good lights and not worrying about mechanical problems (PART FAILURE).
My brother, Ronnie, served as my pit crew during this trip. Car ran
a best time of 10.71 sec. at 121.7 miles per hour. I plan on parking
the car for the holidays and make some tuning adjustments to the chassis
setup. Will be more than ready to race when the track opens after
the holidays.
12/14/02
- Reggie took the Duster to No Problem Raceway Park and had good luck and
bad luck. He won in the first round, running a 10.70 on a 10.65
dial-in. That time would have been much lower had he not let up as
soon as he caught the other car at about the 1000 ft. mark. After
that round the electric motor on the water pump gave out and Reggie
retired for the day. Everything worked perfect, up to that
point. He is very pleased with the new motor!
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